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A Unique Instrumental Malfunction during Robotic Prostatectomy

Over the past decade, the introduction of robotics in the field of medicine has provided a new approach to patients requiring surgery, and both its advantages and disadvantages are currently under study by many groups worldwide. The use of robotics has especially been considered by the urological co...

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Autores principales: Park, Sung Yul, Ahn, Jenny Jin-Kyung, Jeong, Wooju, Ham, Won Sik, Rha, Koon Ho
Formato: Texto
Lenguaje:English
Publicado: Yonsei University College of Medicine 2010
Materias:
Acceso en línea:https://www.ncbi.nlm.nih.gov/pmc/articles/PMC2799975/
https://www.ncbi.nlm.nih.gov/pubmed/20046531
http://dx.doi.org/10.3349/ymj.2010.51.1.148
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author Park, Sung Yul
Ahn, Jenny Jin-Kyung
Jeong, Wooju
Ham, Won Sik
Rha, Koon Ho
author_facet Park, Sung Yul
Ahn, Jenny Jin-Kyung
Jeong, Wooju
Ham, Won Sik
Rha, Koon Ho
author_sort Park, Sung Yul
collection PubMed
description Over the past decade, the introduction of robotics in the field of medicine has provided a new approach to patients requiring surgery, and both its advantages and disadvantages are currently under study by many groups worldwide. The use of robotics has especially been considered by the urological community as a treatment option in radical prostatectomy. The current case report is one in which the da Vinci Surgical System™, with fourth arm use was employed in radical prostatectomy. This case presents a unique occurrence in which a bolt of the Prograsper forcep became loose during an operation, leading to diminished device functionality and later impedance of its removal. A circumstance such as this has not previously been reported, so we introduce for other robotic surgeons our unique instrumental malfunction case during a robotic prostatectomy.
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spelling pubmed-27999752010-01-01 A Unique Instrumental Malfunction during Robotic Prostatectomy Park, Sung Yul Ahn, Jenny Jin-Kyung Jeong, Wooju Ham, Won Sik Rha, Koon Ho Yonsei Med J Case Report Over the past decade, the introduction of robotics in the field of medicine has provided a new approach to patients requiring surgery, and both its advantages and disadvantages are currently under study by many groups worldwide. The use of robotics has especially been considered by the urological community as a treatment option in radical prostatectomy. The current case report is one in which the da Vinci Surgical System™, with fourth arm use was employed in radical prostatectomy. This case presents a unique occurrence in which a bolt of the Prograsper forcep became loose during an operation, leading to diminished device functionality and later impedance of its removal. A circumstance such as this has not previously been reported, so we introduce for other robotic surgeons our unique instrumental malfunction case during a robotic prostatectomy. Yonsei University College of Medicine 2010-01-01 2009-12-29 /pmc/articles/PMC2799975/ /pubmed/20046531 http://dx.doi.org/10.3349/ymj.2010.51.1.148 Text en © Copyright: Yonsei University College of Medicine 2010 http://creativecommons.org/licenses/by-nc/3.0 This is an Open Access article distributed under the terms of the Creative Commons Attribution Non-Commercial License (http://creativecommons.org/licenses/by-nc/3.0) which permits unrestricted noncommercial use, distribution, and reproduction in any medium, provided the original work is properly cited.
spellingShingle Case Report
Park, Sung Yul
Ahn, Jenny Jin-Kyung
Jeong, Wooju
Ham, Won Sik
Rha, Koon Ho
A Unique Instrumental Malfunction during Robotic Prostatectomy
title A Unique Instrumental Malfunction during Robotic Prostatectomy
title_full A Unique Instrumental Malfunction during Robotic Prostatectomy
title_fullStr A Unique Instrumental Malfunction during Robotic Prostatectomy
title_full_unstemmed A Unique Instrumental Malfunction during Robotic Prostatectomy
title_short A Unique Instrumental Malfunction during Robotic Prostatectomy
title_sort unique instrumental malfunction during robotic prostatectomy
topic Case Report
url https://www.ncbi.nlm.nih.gov/pmc/articles/PMC2799975/
https://www.ncbi.nlm.nih.gov/pubmed/20046531
http://dx.doi.org/10.3349/ymj.2010.51.1.148
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