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A Unique Instrumental Malfunction during Robotic Prostatectomy
Over the past decade, the introduction of robotics in the field of medicine has provided a new approach to patients requiring surgery, and both its advantages and disadvantages are currently under study by many groups worldwide. The use of robotics has especially been considered by the urological co...
Autores principales: | , , , , |
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Formato: | Texto |
Lenguaje: | English |
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Yonsei University College of Medicine
2010
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Acceso en línea: | https://www.ncbi.nlm.nih.gov/pmc/articles/PMC2799975/ https://www.ncbi.nlm.nih.gov/pubmed/20046531 http://dx.doi.org/10.3349/ymj.2010.51.1.148 |
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author | Park, Sung Yul Ahn, Jenny Jin-Kyung Jeong, Wooju Ham, Won Sik Rha, Koon Ho |
author_facet | Park, Sung Yul Ahn, Jenny Jin-Kyung Jeong, Wooju Ham, Won Sik Rha, Koon Ho |
author_sort | Park, Sung Yul |
collection | PubMed |
description | Over the past decade, the introduction of robotics in the field of medicine has provided a new approach to patients requiring surgery, and both its advantages and disadvantages are currently under study by many groups worldwide. The use of robotics has especially been considered by the urological community as a treatment option in radical prostatectomy. The current case report is one in which the da Vinci Surgical System™, with fourth arm use was employed in radical prostatectomy. This case presents a unique occurrence in which a bolt of the Prograsper forcep became loose during an operation, leading to diminished device functionality and later impedance of its removal. A circumstance such as this has not previously been reported, so we introduce for other robotic surgeons our unique instrumental malfunction case during a robotic prostatectomy. |
format | Text |
id | pubmed-2799975 |
institution | National Center for Biotechnology Information |
language | English |
publishDate | 2010 |
publisher | Yonsei University College of Medicine |
record_format | MEDLINE/PubMed |
spelling | pubmed-27999752010-01-01 A Unique Instrumental Malfunction during Robotic Prostatectomy Park, Sung Yul Ahn, Jenny Jin-Kyung Jeong, Wooju Ham, Won Sik Rha, Koon Ho Yonsei Med J Case Report Over the past decade, the introduction of robotics in the field of medicine has provided a new approach to patients requiring surgery, and both its advantages and disadvantages are currently under study by many groups worldwide. The use of robotics has especially been considered by the urological community as a treatment option in radical prostatectomy. The current case report is one in which the da Vinci Surgical System™, with fourth arm use was employed in radical prostatectomy. This case presents a unique occurrence in which a bolt of the Prograsper forcep became loose during an operation, leading to diminished device functionality and later impedance of its removal. A circumstance such as this has not previously been reported, so we introduce for other robotic surgeons our unique instrumental malfunction case during a robotic prostatectomy. Yonsei University College of Medicine 2010-01-01 2009-12-29 /pmc/articles/PMC2799975/ /pubmed/20046531 http://dx.doi.org/10.3349/ymj.2010.51.1.148 Text en © Copyright: Yonsei University College of Medicine 2010 http://creativecommons.org/licenses/by-nc/3.0 This is an Open Access article distributed under the terms of the Creative Commons Attribution Non-Commercial License (http://creativecommons.org/licenses/by-nc/3.0) which permits unrestricted noncommercial use, distribution, and reproduction in any medium, provided the original work is properly cited. |
spellingShingle | Case Report Park, Sung Yul Ahn, Jenny Jin-Kyung Jeong, Wooju Ham, Won Sik Rha, Koon Ho A Unique Instrumental Malfunction during Robotic Prostatectomy |
title | A Unique Instrumental Malfunction during Robotic Prostatectomy |
title_full | A Unique Instrumental Malfunction during Robotic Prostatectomy |
title_fullStr | A Unique Instrumental Malfunction during Robotic Prostatectomy |
title_full_unstemmed | A Unique Instrumental Malfunction during Robotic Prostatectomy |
title_short | A Unique Instrumental Malfunction during Robotic Prostatectomy |
title_sort | unique instrumental malfunction during robotic prostatectomy |
topic | Case Report |
url | https://www.ncbi.nlm.nih.gov/pmc/articles/PMC2799975/ https://www.ncbi.nlm.nih.gov/pubmed/20046531 http://dx.doi.org/10.3349/ymj.2010.51.1.148 |
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