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Investigation on the Corrosion of the Elbows in the Flue Gas Cooler of a 600 MW Coal-Fired Power Plant
[Image: see text] Sulfuric acid condensation has long been considered as the major cause of the corrosion issues at the cold-end of coal-fired boilers. However, in a flue gas cooler, where flue gas is cooled to around 90 °C for heat recovery, the influence of chlorides might be underestimated. In th...
Autores principales: | Pan, Peiyuan, Zhou, Weijian, Chen, Heng, Zhang, Naiqiang |
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Formato: | Online Artículo Texto |
Lenguaje: | English |
Publicado: |
American Chemical
Society
2020
|
Acceso en línea: | https://www.ncbi.nlm.nih.gov/pmc/articles/PMC7758941/ https://www.ncbi.nlm.nih.gov/pubmed/33376892 http://dx.doi.org/10.1021/acsomega.0c04838 |
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