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Evaluation of the Pullout Behavior of Pre-Bored Piles Embedded in Rock
The subject of this study is dry process caisson tube method cofferdam (hereinafter called C.T cofferdam). This C.T cofferdam is designed to use the skin friction of the drilled shaft embedded into the rock for stability of buoyancy. A pre-bored pile embedded in the bedrock was pulled out due to the...
Autores principales: | , , , |
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Formato: | Online Artículo Texto |
Lenguaje: | English |
Publicado: |
MDPI
2021
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Materias: | |
Acceso en línea: | https://www.ncbi.nlm.nih.gov/pmc/articles/PMC8509368/ https://www.ncbi.nlm.nih.gov/pubmed/34639990 http://dx.doi.org/10.3390/ma14195593 |
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author | Park, Kyungho Kim, Daehyeon Kim, Gyudeok Lee, Wooyoul |
author_facet | Park, Kyungho Kim, Daehyeon Kim, Gyudeok Lee, Wooyoul |
author_sort | Park, Kyungho |
collection | PubMed |
description | The subject of this study is dry process caisson tube method cofferdam (hereinafter called C.T cofferdam). This C.T cofferdam is designed to use the skin friction of the drilled shaft embedded into the rock for stability of buoyancy. A pre-bored pile embedded in the bedrock was pulled out due to the buoyancy of the C.T cofferdam at the pier (hereinafter called P) 2 of the OO bridges under construction, to which this was applied. In this study, in order to solve this problem, the adhesion force applied with the concept of skin friction and the pre-bored pile of drilled shaft according to domestic and foreign design standards were identified; the on-site pull-out load test was used to calculate the pull-out force; and the skin friction of the drilled shaft and pre-bored pile embedded into the bedrock were compared and analyzed. In addition, the pull-out behavior of the pre-bored pile embedded in the bedrock was analyzed through numerical analysis. The adhesion strength tested in the lab was 881 kN for air curing of concrete and 542 kN for water curing of concrete, and the on-site pull-out test result was 399.7 kN. As a result of the numerical analysis, the material properties of the grout considering the site conditions used revealed that the displacement of the entire structure exceeded the allowable limit and was unstable. This appears to have lowered the adhesion strength due to construction issues such as ground complexity and both seawater and slime treatment, which were not expected at the time of design. |
format | Online Article Text |
id | pubmed-8509368 |
institution | National Center for Biotechnology Information |
language | English |
publishDate | 2021 |
publisher | MDPI |
record_format | MEDLINE/PubMed |
spelling | pubmed-85093682021-10-13 Evaluation of the Pullout Behavior of Pre-Bored Piles Embedded in Rock Park, Kyungho Kim, Daehyeon Kim, Gyudeok Lee, Wooyoul Materials (Basel) Article The subject of this study is dry process caisson tube method cofferdam (hereinafter called C.T cofferdam). This C.T cofferdam is designed to use the skin friction of the drilled shaft embedded into the rock for stability of buoyancy. A pre-bored pile embedded in the bedrock was pulled out due to the buoyancy of the C.T cofferdam at the pier (hereinafter called P) 2 of the OO bridges under construction, to which this was applied. In this study, in order to solve this problem, the adhesion force applied with the concept of skin friction and the pre-bored pile of drilled shaft according to domestic and foreign design standards were identified; the on-site pull-out load test was used to calculate the pull-out force; and the skin friction of the drilled shaft and pre-bored pile embedded into the bedrock were compared and analyzed. In addition, the pull-out behavior of the pre-bored pile embedded in the bedrock was analyzed through numerical analysis. The adhesion strength tested in the lab was 881 kN for air curing of concrete and 542 kN for water curing of concrete, and the on-site pull-out test result was 399.7 kN. As a result of the numerical analysis, the material properties of the grout considering the site conditions used revealed that the displacement of the entire structure exceeded the allowable limit and was unstable. This appears to have lowered the adhesion strength due to construction issues such as ground complexity and both seawater and slime treatment, which were not expected at the time of design. MDPI 2021-09-26 /pmc/articles/PMC8509368/ /pubmed/34639990 http://dx.doi.org/10.3390/ma14195593 Text en © 2021 by the authors. https://creativecommons.org/licenses/by/4.0/Licensee MDPI, Basel, Switzerland. This article is an open access article distributed under the terms and conditions of the Creative Commons Attribution (CC BY) license (https://creativecommons.org/licenses/by/4.0/). |
spellingShingle | Article Park, Kyungho Kim, Daehyeon Kim, Gyudeok Lee, Wooyoul Evaluation of the Pullout Behavior of Pre-Bored Piles Embedded in Rock |
title | Evaluation of the Pullout Behavior of Pre-Bored Piles Embedded in Rock |
title_full | Evaluation of the Pullout Behavior of Pre-Bored Piles Embedded in Rock |
title_fullStr | Evaluation of the Pullout Behavior of Pre-Bored Piles Embedded in Rock |
title_full_unstemmed | Evaluation of the Pullout Behavior of Pre-Bored Piles Embedded in Rock |
title_short | Evaluation of the Pullout Behavior of Pre-Bored Piles Embedded in Rock |
title_sort | evaluation of the pullout behavior of pre-bored piles embedded in rock |
topic | Article |
url | https://www.ncbi.nlm.nih.gov/pmc/articles/PMC8509368/ https://www.ncbi.nlm.nih.gov/pubmed/34639990 http://dx.doi.org/10.3390/ma14195593 |
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