Cargando…

Application of lean Six Sigma methodology using DMAIC approach for the improvement of bogie assembly process in the railcar industry

The quest for waste reduction, quality improvement and operational efficiency during the assembly process of the railcar bogie necessitates this study. Using a case study approach, this study employs the Lean Six Sigma (LSS) approach for process improvement of the railcar bogie assembly process. Pri...

Descripción completa

Detalles Bibliográficos
Autores principales: Daniyan, Ilesanmi, Adeodu, Adefemi, Mpofu, Khumbulani, Maladzhi, Rendani, Kana-Kana Katumba, Mukondeleli Grace
Formato: Online Artículo Texto
Lenguaje:English
Publicado: Elsevier 2022
Materias:
Acceso en línea:https://www.ncbi.nlm.nih.gov/pmc/articles/PMC8917301/
https://www.ncbi.nlm.nih.gov/pubmed/35287321
http://dx.doi.org/10.1016/j.heliyon.2022.e09043
_version_ 1784668519806271488
author Daniyan, Ilesanmi
Adeodu, Adefemi
Mpofu, Khumbulani
Maladzhi, Rendani
Kana-Kana Katumba, Mukondeleli Grace
author_facet Daniyan, Ilesanmi
Adeodu, Adefemi
Mpofu, Khumbulani
Maladzhi, Rendani
Kana-Kana Katumba, Mukondeleli Grace
author_sort Daniyan, Ilesanmi
collection PubMed
description The quest for waste reduction, quality improvement and operational efficiency during the assembly process of the railcar bogie necessitates this study. Using a case study approach, this study employs the Lean Six Sigma (LSS) approach for process improvement of the railcar bogie assembly process. Primary data relating to the assembly process such as the labour and material flow, up and down times were collected at every stage of the assembly operation. The improvement process of the assembly process featured the use of some Lean tools such as the Kaizen, Value Stream Mapping, Pareto chart, Single-Minute Exchange of Die (SMED) and 5S. The investigation of the current assembly process with the use of the LSS technique indicates that the process efficiency is low due to waste generation. The results obtained showed significant improvement in the process cycle efficiency (PCE) by 46.8%, via the implementation of the Kaizen continuous process improvement approach, 27.9% reduction in the lead-time, 59.3% increase in the value added time and 71.9% reduction in the non-value added time after the implementation of the LSS approach. The findings of this work demonstrated the feasibility of the LSS approach for waste minimisation and process performance improvement in a bid to achieve operational excellence in a manufacturing organisation.
format Online
Article
Text
id pubmed-8917301
institution National Center for Biotechnology Information
language English
publishDate 2022
publisher Elsevier
record_format MEDLINE/PubMed
spelling pubmed-89173012022-03-13 Application of lean Six Sigma methodology using DMAIC approach for the improvement of bogie assembly process in the railcar industry Daniyan, Ilesanmi Adeodu, Adefemi Mpofu, Khumbulani Maladzhi, Rendani Kana-Kana Katumba, Mukondeleli Grace Heliyon Research Article The quest for waste reduction, quality improvement and operational efficiency during the assembly process of the railcar bogie necessitates this study. Using a case study approach, this study employs the Lean Six Sigma (LSS) approach for process improvement of the railcar bogie assembly process. Primary data relating to the assembly process such as the labour and material flow, up and down times were collected at every stage of the assembly operation. The improvement process of the assembly process featured the use of some Lean tools such as the Kaizen, Value Stream Mapping, Pareto chart, Single-Minute Exchange of Die (SMED) and 5S. The investigation of the current assembly process with the use of the LSS technique indicates that the process efficiency is low due to waste generation. The results obtained showed significant improvement in the process cycle efficiency (PCE) by 46.8%, via the implementation of the Kaizen continuous process improvement approach, 27.9% reduction in the lead-time, 59.3% increase in the value added time and 71.9% reduction in the non-value added time after the implementation of the LSS approach. The findings of this work demonstrated the feasibility of the LSS approach for waste minimisation and process performance improvement in a bid to achieve operational excellence in a manufacturing organisation. Elsevier 2022-03-05 /pmc/articles/PMC8917301/ /pubmed/35287321 http://dx.doi.org/10.1016/j.heliyon.2022.e09043 Text en © 2022 The Author(s) https://creativecommons.org/licenses/by-nc-nd/4.0/This is an open access article under the CC BY-NC-ND license (http://creativecommons.org/licenses/by-nc-nd/4.0/).
spellingShingle Research Article
Daniyan, Ilesanmi
Adeodu, Adefemi
Mpofu, Khumbulani
Maladzhi, Rendani
Kana-Kana Katumba, Mukondeleli Grace
Application of lean Six Sigma methodology using DMAIC approach for the improvement of bogie assembly process in the railcar industry
title Application of lean Six Sigma methodology using DMAIC approach for the improvement of bogie assembly process in the railcar industry
title_full Application of lean Six Sigma methodology using DMAIC approach for the improvement of bogie assembly process in the railcar industry
title_fullStr Application of lean Six Sigma methodology using DMAIC approach for the improvement of bogie assembly process in the railcar industry
title_full_unstemmed Application of lean Six Sigma methodology using DMAIC approach for the improvement of bogie assembly process in the railcar industry
title_short Application of lean Six Sigma methodology using DMAIC approach for the improvement of bogie assembly process in the railcar industry
title_sort application of lean six sigma methodology using dmaic approach for the improvement of bogie assembly process in the railcar industry
topic Research Article
url https://www.ncbi.nlm.nih.gov/pmc/articles/PMC8917301/
https://www.ncbi.nlm.nih.gov/pubmed/35287321
http://dx.doi.org/10.1016/j.heliyon.2022.e09043
work_keys_str_mv AT daniyanilesanmi applicationofleansixsigmamethodologyusingdmaicapproachfortheimprovementofbogieassemblyprocessintherailcarindustry
AT adeoduadefemi applicationofleansixsigmamethodologyusingdmaicapproachfortheimprovementofbogieassemblyprocessintherailcarindustry
AT mpofukhumbulani applicationofleansixsigmamethodologyusingdmaicapproachfortheimprovementofbogieassemblyprocessintherailcarindustry
AT maladzhirendani applicationofleansixsigmamethodologyusingdmaicapproachfortheimprovementofbogieassemblyprocessintherailcarindustry
AT kanakanakatumbamukondeleligrace applicationofleansixsigmamethodologyusingdmaicapproachfortheimprovementofbogieassemblyprocessintherailcarindustry