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The industrial feasibility of low temperature DeNO(x) in the presence of SO(x): a project case in a medium coking plant

Catalyst poisoning by SO(x) has hindered the industrial application of selective catalytic reduction (SCR) technology for the DeNO(x) of low temperature flue gas for many decades. The current engineering process of placing the SCR unit after the desulphurization and dedusting units can lead to high...

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Autores principales: Li, Changming, Yu, Jian, He, Yi, Yu, Chao, Li, Ping, Wang, Chao, Huang, Fulin, Gao, Shiqiu
Formato: Online Artículo Texto
Lenguaje:English
Publicado: The Royal Society of Chemistry 2018
Materias:
Acceso en línea:https://www.ncbi.nlm.nih.gov/pmc/articles/PMC9080530/
https://www.ncbi.nlm.nih.gov/pubmed/35541112
http://dx.doi.org/10.1039/c8ra02767f
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author Li, Changming
Yu, Jian
He, Yi
Yu, Chao
Li, Ping
Wang, Chao
Huang, Fulin
Gao, Shiqiu
author_facet Li, Changming
Yu, Jian
He, Yi
Yu, Chao
Li, Ping
Wang, Chao
Huang, Fulin
Gao, Shiqiu
author_sort Li, Changming
collection PubMed
description Catalyst poisoning by SO(x) has hindered the industrial application of selective catalytic reduction (SCR) technology for the DeNO(x) of low temperature flue gas for many decades. The current engineering process of placing the SCR unit after the desulphurization and dedusting units can lead to high project and operational costs owing to low DeNO(x) efficiency at low temperatures. Based on our previous pilot results, a DeNO(x) project case was built before the desulfurization unit in a medium coking plant to explore the industrial feasibility of low temperature DeNO(x) in the presence of SO(x). A new engineering process was considered and designed to overcome the problem of SO(x), including the elimination of SO(3) with NH(3) before the SCR reactor, the filtration of ash by a foam metal plate and in situ regeneration technology. The project case could run continuously for six months with above 70% DeNO(x) efficiency and less than 10 ppm NH(3) slip at 250 °C and a space velocity of 4000 h(−1) in the presence of 260–300 mg m(−3) SO(x). The activity loss for the catalyst itself was not obvious after it had been running for six months, but blocking of the honeycomb channels by the sedimentary ash on the honeycomb catalyst modules owing to the low linear velocity resulted in decreased DeNO(x) efficiency and an increased pressure drop. A improved DeNO(x) process with gravitational dust collectors was also proposed to upgrade the present DeNO(x) project case for further continuous and stable operation.
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spelling pubmed-90805302022-05-09 The industrial feasibility of low temperature DeNO(x) in the presence of SO(x): a project case in a medium coking plant Li, Changming Yu, Jian He, Yi Yu, Chao Li, Ping Wang, Chao Huang, Fulin Gao, Shiqiu RSC Adv Chemistry Catalyst poisoning by SO(x) has hindered the industrial application of selective catalytic reduction (SCR) technology for the DeNO(x) of low temperature flue gas for many decades. The current engineering process of placing the SCR unit after the desulphurization and dedusting units can lead to high project and operational costs owing to low DeNO(x) efficiency at low temperatures. Based on our previous pilot results, a DeNO(x) project case was built before the desulfurization unit in a medium coking plant to explore the industrial feasibility of low temperature DeNO(x) in the presence of SO(x). A new engineering process was considered and designed to overcome the problem of SO(x), including the elimination of SO(3) with NH(3) before the SCR reactor, the filtration of ash by a foam metal plate and in situ regeneration technology. The project case could run continuously for six months with above 70% DeNO(x) efficiency and less than 10 ppm NH(3) slip at 250 °C and a space velocity of 4000 h(−1) in the presence of 260–300 mg m(−3) SO(x). The activity loss for the catalyst itself was not obvious after it had been running for six months, but blocking of the honeycomb channels by the sedimentary ash on the honeycomb catalyst modules owing to the low linear velocity resulted in decreased DeNO(x) efficiency and an increased pressure drop. A improved DeNO(x) process with gravitational dust collectors was also proposed to upgrade the present DeNO(x) project case for further continuous and stable operation. The Royal Society of Chemistry 2018-05-18 /pmc/articles/PMC9080530/ /pubmed/35541112 http://dx.doi.org/10.1039/c8ra02767f Text en This journal is © The Royal Society of Chemistry https://creativecommons.org/licenses/by/3.0/
spellingShingle Chemistry
Li, Changming
Yu, Jian
He, Yi
Yu, Chao
Li, Ping
Wang, Chao
Huang, Fulin
Gao, Shiqiu
The industrial feasibility of low temperature DeNO(x) in the presence of SO(x): a project case in a medium coking plant
title The industrial feasibility of low temperature DeNO(x) in the presence of SO(x): a project case in a medium coking plant
title_full The industrial feasibility of low temperature DeNO(x) in the presence of SO(x): a project case in a medium coking plant
title_fullStr The industrial feasibility of low temperature DeNO(x) in the presence of SO(x): a project case in a medium coking plant
title_full_unstemmed The industrial feasibility of low temperature DeNO(x) in the presence of SO(x): a project case in a medium coking plant
title_short The industrial feasibility of low temperature DeNO(x) in the presence of SO(x): a project case in a medium coking plant
title_sort industrial feasibility of low temperature deno(x) in the presence of so(x): a project case in a medium coking plant
topic Chemistry
url https://www.ncbi.nlm.nih.gov/pmc/articles/PMC9080530/
https://www.ncbi.nlm.nih.gov/pubmed/35541112
http://dx.doi.org/10.1039/c8ra02767f
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